Case History

Oklahoma Operator Reduces the Costs and Risks of Snubbing In Production Tubing with the Atlas Dissolvable Packer™

Time & Location

Q4 2021 – SCOOP/STACK Oklahoma

Well Conditions

BHT 250°F BHP 6,400 psi Freshwater

Challenge

Operator wanted to install the tubing deeper into the curve of a horizontal well for an annular gas lift operation than they felt comfortable with while running a traditional packer or without a snubbing unit.

Solution

An Atlas Dissolvable Packer™ was installed by wireline at a depth of 11,030’ at 70° deviation and held 3000psi pressure from below. Once tubing was installed, the integral pump-out plug was expended right on the target pinning pressure allowing production to flow through the Atlas™ bore.

Value

By placing the end-of-tubing deeper into the curve, the operator was able to increase drawdown and production by 11% vs. In addition to production improvements, the operator saved money by eliminating costly snubbing services.
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